RC Timer 5010 Motor problem

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I have the same problem with two motors. Flight time 0 minutes. :(
dead on arrival.
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Just check again the bullet connectors. It looks like cold soldering.
Usualy this is solved by resoldering the connectors.
You can use a multimeter (measure resistance) to measure between any of the 3 connectors and find the one that has big resistance with the other two.

mirceacul
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Maybe you need to tighten the prop screw which appears to be omitted?

Kabab
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Yes sure... ;) At the time, I bought these motors, rctimer didn't have gimbal motors. :) I had to wind them myself. They are now using the same housings for the gimbal and flying motors. The difference is the soldering board and of course the winding. The ESCs where not flashed correctly with the simonK firmware. Rctimer support couldn't care less. :(

FlyRotor
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dude, you bought gimbal motors.
their usage is for gimbals and not for flying -.-

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